so here's the thing.
i have 2 x 250cc bikes now both making the same rattling - deto noise......
1 has a PVL - set at 2.3 BTDC
1 has a standard yamaha ign set at factory BTDC
one has a 36mm carby
1 has a 34mm carby
1 rebuilt motor
1 original motor
NOw here's the thing, they were jetted seperately and by differant people and with a plug chop there looks to be tan and plenty of gas on the main jet on BOTH.
And they both sound clean and crisp off idle on the stand.
NOw this is where it goes pear shaped, after the first FT lap or 30 sec, they both rattle from what sounds like in the head/ barrell like a can of spray paint. and i mean rattle ugley although it seems to get noisey as they warm up and is only under riding throttle.
I have stuffed about with the timing and main jets and results stay prity much the same. There must be a common denominator as the bikes are unrelated so there is no duplication of a mechanical error.
Although they were ridden seperately, and 6 months apart , the fuel came from the same bowser outlet , as i happened to have a empty can on me at the time. It was shell V power or what ever they call there 98 at both times. LAter yesterday after we had a tune up day bike 2 displayed the same characteristics as its brother had 6 months earlier at a race day. Later in the day i drained the tank and used a mix of BP 98 and TTS the pinging/ rattle had moved from across the range under load to just the bottom to mid under load and went away at full revs, throttle. so i suspect its in the Fuels burn or the timing of the burn.
The motors are stock so the amount or style of fuel is my problem i suspect. What does my head in is, both the bikes are displaying the same issue. "Rattle can in the motor' albeit now i have got it down to the low end - loaded. Late in the day After about 6 laps i think it nipped up So i pulled in , (will pull it down this week to see what was going on there) as it warmed up, and maybe up the pilot incase its leaning off the gas. But these bikes are to far removed to be displaying the same fault based only on set up. iT has to be a fuel related issue in quality or quantiy characterised by the Shell or BP 98 that has changed the previous baselines that worked.
Question anyone else seen this change and if so what correction did you make to move or solve the issue ?
What concrete ( not guesses please ) adjustments should be made to chase out the problem.
I plan to pull them both down in the next week or so and record them separately to see what is mechanically the same and what if anythign is differant in the barrel and head, squishes and comp etc. Incase there is a need to refer to this data and make changes.