Funny you mention base gasket Lozza, I put a new one on, but it was in a cometic kit and was tin as opposed to paper genuine ktm one.
At the time of instillation it
looked thinner.
I don't feel there is an air leak as it runs fine otherwise, no over rev, high idles that kind of stuff.
It has only started after the ring change, nothing else has changed and 2 weeks ago was running fine.
I would have thought that a main jet that was 2 steps richer, would offset any lean needle position at 3/4 to wfo throttle settings.
Will get pics of plug and piston tonight.