YZ125K Ride Report:
Day one, got into the bush and went for my first ride on the bike. I have warmed it up at home a few times but i still needed to run it in under load, so i puttered around a bit. First pic shows the setup i have for getting it all out there. Intial feel of the bike was great. Suspension worked well and bike felt good. A lot of smoke and spooge coming out but i need to open it up a bit to find out whats what. OK, second pic is a minute before bike broke down. I took off again and got 20 seconds down the track and it died like when you run out of juice. Checked fuel tap...noop. A wiggle here and a look there, but she would not start. Pushed it back to car and went home to wash her down and investigate. Ended up being NGK Iridium plug. Just 30 minutes old and packed up. Maybe because of the oily bike.
I checked timing.. a bit off.. it was 1.4mm btdc. I reset to PVL recommendations at 1.2mm. Next was the spooge. I had put a 50 pilot in as thats what the Yamaha Race Report said was the hot ticket for the upgraded 36VM. The modern day 36VM comes prejetted with a 35 pilot. I put the 35 back in and at 1 - 1.5 turns out it cleared up the roughness and got rid of the smoke. Time for another test ride.
Day two test ride. Started first kick on the choke and run well. Took a minute to clear its throat and then we were away. I gave it a half arsed attempt at final run in but it was good enough for me and i started opening up. Bike now rips. Still needs some jetting but getting there. In first it can sound like four stroke valve bounce when i rev it hard sometimes. The suspension is great and really handled the whoops and sand. I have not hit any jumps yet so my forks only showed im using about 7 inches of the 12. I may have to take a whisker of oil out of the forks if i cant get full compression. Photo 3 shows the tracks im running. They are all whooped out everywhere. On the long fire tracks i could get 6th gear wide open on the whoops and the bike felt really stable. Fourth photo is when i noticed radiator fluid coming out the overflow. It wasnt steaming, it was just coming out. I headed back to the car with another 30 minutes of testing done. The rad needed 350ml of fluid when i got home. I'm not sure if i had the cap on tight. I will take my genuine cap and some fluid out with me next time.
Brakes have bedded in and i have now used up all my adjustments. So i have to pull the levers off at the hubs and move them a couple of notches. Bike now needs checking over, tightening everything and getting ready for another run.
Cheers,
Alex